Category Archives: Space Flight

11 November 1966, 20:46:33.419 UTC, T minus Zero

Gemini XII lifts off from LC-19 at 2:21:04 p.m., EST, 11 November 1966. (NASA)
Gemini XII lifts off from LC-19 at 3:46:33 p.m., EST, 11 November 1966. (NASA)

11 November 1966: Gemini 12 lifted off from Launch Complex 19 at the Cape Canaveral Air Force Station, Florida, at 3:36.33.419 p.m., Eastern Standard Time. Two NASA Astronauts, Captain James A Lovell, Jr., United States Navy, and Major Edwin E. (“Buzz”) Aldrin, Jr., United States Air Force, were the crew. This was the second space flight for Lovell, who had previously flown on Gemini VII, and would later serve as Command Module Pilot on Apollo 8 and Mission Commander on Apollo 13. It was Aldrin’s first space flight. He would later be the Lunar Module Pilot of Apollo 11, and was the second human to set foot of the surface of the Moon.

The Gemini 12 mission was to rendezvous and docking with an Agena Target Vehicle, which had been launched from Launch Complex 14, 1 hour, 38 minutes, 34.731 seconds earlier by an Atlas Standard Launch Vehicle (SLV-3), and placed in a nearly circular orbit with a perigee of 163 nautical miles (187.6 statute miles/301.9 kilometers) and apogee of 156 nautical miles (179.5 statute miles/288.9 kilometers).

Artist’s concept of Gemini spacecraft, 3 January 1962. (NASA-S-65-893)

The two-man Gemini spacecraft was built by the McDonnell Aircraft Corporation of St. Louis, the same company that built the earlier Mercury space capsule. The spacecraft consisted of a reentry module and an adapter section. It had an overall length of 19 feet (5.791 meters) and a diameter of 10 feet (3.048 meters) at the base of the adapter section. The reentry module was 11 feet (3.353 meters) long with a diameter of 7.5 feet (2.347 meters). The weight of the Gemini varied from ship to ship, but Spacecraft 12 weighed 8,296.47 pounds (3,763.22 kilograms) at liftoff.

The Titan II GLV was a “man-rated” variant of the Martin SM-68B intercontinental ballistic missile. It was assembled at Martin Marietta’s Middle River, Maryland plant so as not to interfere with the production of the ICBM at Denver, Colorado. Twelve GLVs were ordered by the Air Force for the Gemini Program.

The Titan II GLV was a two-stage, liquid-fueled rocket. The first stage was 63 feet (19.202 meters) long with a diameter of 10 feet (3.048 meters). The second stage was 27 feet (8.230 meters) long, with the same diameter. The 1st stage was powered by an Aerojet Engineering Corporation LR-87-7 engine which combined two combustion chambers and exhaust nozzles with a single turbopump unit. The engine was fueled by a hypergolic combination of hydrazine and nitrogen tetroxide. Ignition occurred spontaneously as the two components were combined in the combustion chambers. The LR-87-7 produced 430,000 pounds of thrust (1,912.74 kilonewtons).¹ It was not throttled and could not be shut down and restarted. The 2nd stage used an Aerojet LR-91 engine which produced 100,000 pounds of thrust (444.82 kilonewtons).²

The Gemini/Titan II GLV combination had a total height of 109 feet (33.223 meters) and weighed approximately 340,000 pounds (154,220 kilograms) when fueled.³

Astronaut Buzz Aldrin standing in the open hatch of Gemini XII in Earth orbit. (NASA)

Gemini XII was the tenth and last flight of the Gemini program. The purpose of this mission was to test rendezvous and docking with an orbiting Agena Target Docking Vehicle and to test extravehicular activity (“EVA,” or “space walk”) procedures. Both of these were crucial parts of the upcoming Apollo program and previous problems would have to be resolved before the manned space flight projects could move to the next phase.

Buzz Aldrin had made a special study of EVA factors, and his three “space walks,” totaling 5 hours, 30 minutes, were highly successful. The rendezvous and docking was flown manually because of a computer problem, but was successful. In addition to these primary objectives, a number of scientific experiments were performed by the two astronauts.

Gemini XII is tethered to the Agena TDV, in Earth orbit over the southwest United States and northern Mexico. (NASA)
Gemini XII is tethered to the Agena TDV, in Earth orbit over the southwest United States and northern Mexico. (NASA)

Gemini XII reentered Earth’s atmosphere and splashed down in the Atlantic Ocean, just 3.8 nautical miles (4.4 statute miles/7.0 kilometers) from the planned target point. Lovell and Aldrin were hoisted aboard a Sikorsky SH-3A Sea King helicopter and transported to the primary recovery ship, USS Wasp (CVS-18). The total duration of the flight was 3 days, 22 hours, 34 minutes, 31 seconds.

Gemini 12 splashes down in the Atlantic Ocean. (NASA S66-59936)
Gemini XII astronauts Major Edwin E. Aldrin, Jr., USAF, and Captain James A. Lovell, Jr., USN, arrive aboard USS Wasp (CVS-18), 15 November 1966. (NASA)

¹ Post-flight analysis gave the total average thrust of GLV-12’s first stage as 458,905 pounds of thrust (2,041.31 kilonewtons)

² Post-flight analysis gave the total average thrust of GLV-12’s second stage as 99,296 pounds of thrust (441.69 kilonewtons)

³ Gemini XII/Titan II GLV (GLV-12) weighed 345,710 pounds (156,811 kilograms) at Stage I ignition.

© 2018, Bryan R. Swopes

9 November 1967, 12:00:01.263 UTC, T plus 0.263

Apollo 4 Saturn V (AS-501) on the launch pad at sunset, the evening before launch, 8 November 1967. (NASA)
Apollo 4 Saturn V (AS-501) on the launch pad at sunset, the evening before launch, 8 November 1967. (NASA)

9 November 1967: The first flight of a Saturn V took place when the unmanned Apollo 4/Saturn V (AS-501) was launched from Pad 39A at the Kennedy Space Center, Cape Canaveral, Florida. The rocket lifted off at 12:00:01.263 UTC.

AS-501 consisted of the first Saturn V launch vehicle, SA-501, with Apollo Spacecraft 017 (a Block I vehicle with Block II upgrades), and included the Launch Escape Tower, Command Module, Service Module, Lunar Module Adapter, and Lunar Module Test Article LTA-10R).

The Saturn V rocket was a three-stage, liquid-fueled heavy launch vehicle. Fully assembled with the Apollo Command and Service Module, it stood 363 feet, 0.15 inches (110.64621 meters) tall, from the tip of the escape tower to the bottom of the F-1 engines. The first and second stages were 33 feet, 1.2 inches (10.089 meters) in diameter. Fully loaded and fueled the rocket weighed 6,200,000 pounds (2,948,350 kilograms).¹ It could lift a payload of 260,000 pounds (117,934 kilograms) to Low Earth Orbit.

The first stage was designated S-IC. It was designed to lift the entire rocket to an altitude of 220,000 feet (67,056 meters) and accelerate to a speed of more than 5,100 miles per hour (8,280 kilometers per hour). The S-IC stage was built by Boeing at the Michoud Assembly Facility, New Orleans, Louisiana. It was 138 feet (42.062 meters) tall and had an empty weight of 290,000 pounds (131,542 kilograms). Fully fueled with 203,400 gallons (770,000 liters) of RP-1 and 318,065 gallons (1,204,000 liters) of liquid oxygen, the stage weighed 5,100,000 pounds (2,131,322 kilograms). It was propelled by five Rocketdyne F-1 engines, producing 1,522,000 pounds of thrust, each, for a total of 7,610,000 pounds of thrust at Sea Level.² These engines were ignited seven seconds prior to lift off and the outer four burned for 168 seconds. The center engine was shut down after 142 seconds to reduce the rate of acceleration. The F-1 engines were built by the Rocketdyne Division of North American Aviation at Canoga Park, California.

A Rocketdyne F-1 engine is being installed on a Saturn S-IC first stage. (NASA)

The S-II second stage was built by North American Aviation at Seal Beach, California. It was 81 feet, 7 inches (24.87 meters) tall and had the same diameter as the first stage. The second stage weighed 80,000 pounds (36,000 kilograms) empty and 1,060,000 pounds loaded. The propellant for the S-II was liquid hydrogen and liquid oxygen. The stage was powered by five Rocketdyne J-2 engines, also built at Canoga Park. Each engine produced 232,250 pounds of thrust, and combined, 1,161,250 pounds of thrust.³

The Saturn V third stage was designated S-IVB. It was built by Douglas Aircraft Company at Huntington Beach, California. The S-IVB was 58 feet, 7 inches (17.86 meters) tall with a diameter of 21 feet, 8 inches (6.604 meters). It had a dry weight of 23,000 pounds (10,000 kilograms) and fully fueled weighed 262,000 pounds. The third stage had one J-2 engine and also used liquid hydrogen and liquid oxygen for propellant.⁴ The S-IVB would place the Command and Service Module into Low Earth Orbit, then, when all was ready, the J-2 would be restarted for the Trans Lunar Injection.

Eighteen Saturn V rockets were built. They were the most powerful machines ever built by man.

Apollo 4 Saturn V AS-501 lifts off at 12:00:01 UTC, 9 November 1967. (NASA)
Apollo 4 Saturn V (AS-501) lifts off at 12:00:01 UTC, 9 November 1967. (NASA)

¹ The AS-501 total vehicle mass at First Motion was 6,137,868 pounds (2,784,090 kilograms).

²  Post-flight analysis gave the total thrust of AS-501’s S-IC stage as 7,728,734.5 pounds of thrust (34,379.1 kilonewtons).

³ Post-flight analysis gave the total thrust of AS-501’s S-II stage as 1,086,396 pounds of thrust (4,832.5 kilonewtons).

⁴ Post-flight analysis gave the total thrust of AS-501’s S-IVB stage as 222,384 pounds of thrust (989.2 kilonewtons) during the first burn; 224,001 pounds (996.4 kilonewtons) during the second burn.

© 2017, Bryan R. Swopes

9 November 1962

McKAY, John B. (Jack) with X-15 56-6672, 13 March 1964 9 November 1962: Flight 74 of the X-15 Program was the Number Two aircraft’s 31st flight. X-15 56-6671 was carried aloft by Balls 8, the Boeing NB-52B Stratofortress, 53-008, for launch over Mud Lake, Nevada. NASA test pilot John Barron (“Jack”) McKay was to take the rocketplane to 125,000 feet at Mach 5.5 to investigate the stability and handling of the X-15 with the lower half of the ventral fin removed, and to investigate aerodynamic boundary layer phenomena.

North American Aviation X-15 56-6671 under the right wing of a B-52 Stratofortress at 45,000 feet. (NASA)
North American Aviation X-15 56-6671 under the right wing of a B-52 Stratofortress at 45,000 feet. (NASA)

The B-52 mothership dropped Jack McKay and the X-15 right on schedule at 10:23:07.0 a.m., local time, from an altitude of 45,000 feet (13,716 meters) and speed of approximately 450 knots (833 kilometers per hour). McKay advanced the throttle to ignite the Reaction Motors XLR99-RM-1 rocket engine. It fired immediately but when McKay advanced the throttle for the full 57,000 pounds of thrust, the engine remained at just 30%.

The X-15 could have flown back to Edwards Air Force Base, about 200 miles (320 kilometers) to the south, but with the engine not responding to the throttle, it was uncertain that it would continue running. The decision was made to make an emergency landing at Mud Lake.

Having reached a peak altitude of 53,950 feet (16,444 meters) and Mach 1.49 (1,109 miles per hour/1,785 kilometers per hour), Jack McKay continued to circle the lake burning off propellants as he lost altitude. The engine was shut down at 70.5 seconds. McKay positioned the aircraft for landing as he continued to dump unused propellant and liquid oxygen, but a considerable amount remained on board.

As he neared touchdown, he tried to lower the flaps but they did not deploy. The X-15 touched down on the dry lake bed at 296 miles per hour (476.4 kilometers per hour), 66 miles per hour (106 kilometers per hour) faster than normal.

Duration of the flight from air launch to touchdown was 6 minutes, 31.1 seconds.

The high speed and extra weight caused the X-15’s rear skids to hit harder than normal. When the nose wheels hit, a rebound effect placed even higher loads on the rear struts. At the same time, with the elevators in an extreme nose-up position, the higher aerodynamic loads pushed the skids deeper into the lake bed. This higher loading caused the left rear strut to collapse. The X-15 rolled to the left and the left elevator dug into the lake bed. This caused the aircraft to start sliding to the left. Jack McKay jettisoned the canopy and as the right wing tip dug into the surface, the X-15 flipped over and came to rest upside down.

A Piasecki H-21 rescue helicopter lands near the overturned X-15 at Mud Lake, 9 November 1961. (NASA)
A Piasecki H-21 rescue helicopter lands near the overturned X-15 at Mud Lake, 9 November 1961. (NASA)
The X-15 rolled over when the left landing skid collapsed because of the high-speed, overweight emergency landing at Mud Lake, Nevada. Jack McKay was trapped in the cockpit and suffered serious spinal injuries. (NASA)
The X-15 rolled over when the left landing skid collapsed because of the high-speed, overweight emergency landing at Mud Lake, Nevada. Jack McKay was trapped in the cockpit and suffered serious spinal injuries. (NASA)
The Number Two X-15, 56-6671, lies upside down and severely damaged at Mud Lake, Nevada, 9 November 1962. (NASA)
The Number Two X-15, 56-6671, lies upside down and severely damaged at Mud Lake, Nevada, 9 November 1962. (NASA)

McKay was seriously injured. He was trapped in the upside down X-15 and was in danger from the vapors of the ammonia propellants and liquid oxygen. An H-21 rescue helicopter hovered overhead to blow the vapor away.

Prior to the flight, an Air Force C-130 had brought a fire engine and crew to standby at Mud Lake, returned to Edwards and picked up a second fire engine and its crew, then remained airborne should an emergency landing be made at another intermediate dry lake.

These propositioned emergency assets were able to rescue McKay and to transport him to the hospital back at Edwards.

McKay eventually recovered sufficiently to return to flight status, but ultimately his injuries forced him to retire.

The Number Two X-15 was severely damaged. It was taken back to North American and was rebuilt into the X-15A-2, intended to reach speeds up to Mach 8. It would be more than a year and a half before it flew again.

North American Aviation X-15A-2 56-6671, after a 19-month repair, redesign and modification program. The fuselage was lengthened, additional propellant and reaction control tanks installed internally, the nose wheel and rear landing skid struts lengthened, and external tanks installed. (NASA)
North American Aviation X-15A-2 56-6671, after a 19-month repair, redesign and modification program. The fuselage was lengthened, additional propellant and reaction control tanks installed internally, the nose wheel and rear landing skid struts lengthened, and external tanks installed. (NASA)

© 2016, Bryan R. Swopes

9 November 1961

Major Robert M. White was the first pilot to exceed Mach 4, Mach 5, and on 9 November 1961, he flew to Mach 6.04. (NASA)
Major Robert M. White was the first pilot to exceed Mach 4, Mach 5, and on 9 November 1961, he flew to Mach 6.04. (U.S. Air Force)

9 November 1961: Major Robert M. White, U.S. Air Force, became the first pilot to fly faster than Mach 6 when he flew the number two North American Aviation X-15 hypersonic research rocketplane, 56-6671, to Mach 6.04.

This was the 45th flight of the X-15 program, and Bob White’s 11th flight. The purpose of this test flight was to accelerate 56-6671 to its maximum velocity, to gather data about aerodynamic heating at hypersonic speeds, and to evaluate the rocketplane’s stability and handling.

Boeing NB-52A Stratofortress 52-003 carries a North American Aviation X-15 piloted by Major Bob White. (NASA)
Boeing NB-52A Stratofortress 52-003 carries a North American Aviation X-15 piloted by Major Bob White. (NASA)

The X-15 was carried to approximately 45,000 feet (13,716 meters) while mounted to a pylon under the right wing of the “mothership,” a Boeing NB-52B Stratofortress, 52-008, nicknamed Balls 8. White was dropped over Mud Lake, Nevada, approximately 200 miles (322 kilometers) north of Edwards Air Force Base. Once clear of the B-52, he ignited the Reaction Motors XLR99-RM-1 rocket engine, and with it producing 57,000 pounds of thrust (253.549 kilonewtons) at full throttle, the X-15 accelerated for 86.9 seconds. The rocketplane reached a peak altitude of 101,600 feet (30,968 meters). Its speed was Mach 6.04 (4,094 miles per hour/6,589 kilometers per hour).

White stated in his post-flight report, “When I leveled off at about 101,000 feet, I made a little downward pressure [on the control stick], because I didn’t want to be climbing. I remember . . . going along watching that [Mach] meter reading roughly 6,000 feet per second, [and] saying to myself, ‘Go, go, go, go!’ We did just crack it, because we knew that bringing all the proper things together, we could or should get just about Mach 6.”

In order to achieve the goal, the flight plan called for pushing the LR-99 to the point of exhaustion instead of manually shutting down the engine at an arbitrary point. White said, “The shutdown seemed to be a little bit different this time, compared with a shutdown by closing the throttle. It seemed to occur over a longer time interval.” 

The X-15 Rocket Plane: Flying the First Wings into Space, by Michelle Evans, University of Nebraska Press, Lincoln and London, 2013, Chapter 3 at Page 87.

The number two North American Aviation X-15, 56-6671, is dropped from the Boeing NB-52A Stratofortress, 52-003. The XLR99 rocket engine is just igniting. Frost from the cryogenic fuels coats the fuselage. (NASA)
The number two North American Aviation X-15, 56-6671, is dropped from the Boeing NB-52A Stratofortress, 52-003. The XLR99 rocket engine is just igniting. Frost from the cryogenic fuels coats the fuselage. (NASA)

“The airplane really did get hot on those flights. Temperatures in excess of 1,300 °F. were recorded. Parts of the airplane glowed cherry red and softened up a bit during those flights. The airplane got so damned hot that it popped and banged like an old iron stove. It spewed smoke out of its bowels and it twitched like frog legs in a skillet. But it survived.”

At the Edge of Space: The X-15 Flight Program, by Milton O. Thompson, Smithsonian Institution Press, Washington, 1992, at Page 98.

North American Aviation X-15 56-6671 accelerates after the XLR99 engine is ignited. (NASA)
North American Aviation X-15 56-6671 accelerates after the XLR99 engine is ignited. (NASA)

As the X-15 decelerated through Mach 2.4, the right side windshield shattered, leaving it completely opaque. On Bob White’s previous flight, the left windshield had also broken. Fortunately, in both cases, only the outer layer of the dual pane glass broke. The reduced visibility made the approach difficult to judge, but White made a successful landing, touching down on Rogers Dry Lake after a flight of 9 minutes, 31.2 seconds duration.

The number three North American Aviation X-15 rocketplane, 56-6672, just before touchdown on Rogers Dry Lake. A Lockheed F-104 Starfighter chase plane escorts it. The green smoke helps the pilots judge wind direction and speed. Frost on the X-15's belly shows residual propellants in the tanks. (NASA)
The number three North American Aviation X-15 rocketplane, 56-6672, just before touchdown on Rogers Dry Lake. A Lockheed F-104 Starfighter chase plane escorts it. The green smoke helps the pilots judge wind direction and speed. Frost on the X-15’s belly shows residual propellants in the tanks. (NASA)
NASA ET62-0270
The shattered windshield of X-15 56-6671, 9 November 1961. (NASA)

A P-51 Mustang fighter pilot in World War II, Robert M. White was shot down on his 52nd combat mission in February 1945 and captured. He was held as a prisoner of war until the war in Europe came to an end in April 1945. White was recalled to active duty during the Korean War. He was a graduate of the Air Force Experimental Test Pilot School and flew tests of many aircraft at Edwards before entering the X-15 program.

Major White had been the first pilot to fly faster than Mach 4, Mach 5 and Mach 6. He was the first to fly over 200,000 feet, then over 300,000 feet. He made at total of sixteen X-15 flights.

Major Robert M. White, U.S. Air Force, with one of the three North American Aviation X-15s on Rogers Dry Lake, 1961. (NASA)
Major Robert M. White, U.S. Air Force, with one of the three North American Aviation X-15s on Rogers Dry Lake, 1961. (NASA)

After leaving the X-15 program, Bob White returned to operational duties. Later, he flew 70 combat missions over North Vietnam in the Republic F-105 Thunderchief supersonic fighter bomber, including leading the attack against the Paul Doumer Bridge at Hanoi, 11 August 1967, for which he was awarded the Air Force Cross. He next went to Wright-Patterson AFB where he was director of the F-15 Eagle systems program. He returned to Edwards AFB as commander of the Air Force Flight Test Center. White was promoted to Major General in 1975.

General White retired from the U.S. Air Force in 1981. He died 10 March 2010.

A North American Aviation support crew deactivates X-15 56-6671 on Rogers Dry Lake after a flight, while the mothership, NB-52A Stratofortress 52-003 flies overhead. (NASA)
A North American Aviation support crew deactivates X-15 56-6671 on Rogers Dry Lake after a flight, while the mothership, NB-52A Stratofortress 52-003 flies overhead. (NASA)

© 2016, Bryan R. Swopes

5 November 1959

The Number 2 X-15, 56-6671, broke in half when it made an emergency landing while still partially loaded with propellants. (NASA)
The Number 2 X-15, 56-6671, broke in half when it made an emergency landing while still partially loaded with propellants. (NASA)

5 November 1959: During his fourth X-15 flight—the third in the Number Two ship, 56-6671—North American Aviation chief test pilot Albert Scott Crossfield made an emergency landing at Rosamond Dry Lake after one of the two Reaction Motors XLR11-RM-13 rocket engines exploded, causing an engine compartment fire.

The X-15 had been launched by the Boeing NB-52A Stratofortress, 52-003, at 0.82 Mach and approximately 45,000 feet (13,716 meters) over Bouquet Canyon Reservoir, about 35 miles (56 kilometers) southwest of Edwards Air Force Base. Scott Crossfield ignited both XLR11 rocket engines and began to accelerate and climb, but one of four combustion chambers of the lower engine exploded almost immediately. He shut both engines down after 11.7 seconds. Crossfield kept the rocketplane in a level attitude for the 114 seconds it took to jettison the liquid oxygen and water-alcohol propellants to lighten the X-15 for the landing. The tanks could not fully drain and the aircraft remained approximately 1,000 pounds (455 kilograms) overweight.

The X-15 approached the emergency landing site at Rosamond Dry Lake, about ten miles (16 kilometers) southwest of Edwards, while Major Robert M. White, flying a Lockheed F-104 chase plane, called out Crossfield’s distance from the dry lake and his altitude. As he neared the touch down point, Crossfield raised the X-15’s nose to decelerate.

“I lowered the skids and nose wheel, pulled the flaps, and felt for the lake bed.

“The skids dug in gently. The nose wheel slammed down hard and the ship plowed across the desert floor, slowing much faster than usual. Then she came to a complete stop within 1500 feet instead of the usual 5000 feet. Something was wrong; the skids failed, I was sure. . . Quickly I scrambled out of the cockpit. What I saw almost broke my heart. The fuselage had buckled immediately aft of the cockpit, two hundred and thirty inches back from the nose. Her belly had dragged in the sand, causing the abrupt deceleration on the lake. The rocket chambers which had exploded at launch were a shambles.”

Always Another Dawn: The Story of a Rocket Test Pilot, by A. Scott Crossfield and Clay Blair, Jr., The World Publishing Company, Cleveland and New York, 1960, Chapter 41 at Pages 383–384.

The scene at Rosamond Dry Lake after Scott Crossfield's emergency landing after an engine explosion. (NASA)
The scene at Rosamond Dry Lake after Scott Crossfield’s emergency landing following an engine explosion. (NASA)

It was determined that the engine had exploded due to an ignition failure, a relatively simple problem not connected to the design of the X-15. But there remained the question as to why the rocketplane had broken in half. The investigation found that the rapid extension of the nose wheel strut when lowered caused the oil inside the strut to foam and vaporize, providing almost no shock absorption. This was corrected and the check list changed to lower the gear sooner.

The total duration of this flight was 5 minutes, 28.0 seconds. The peak altitude was 45,462 feet (13,857 meters) and the maximum speed was 660 miles per hour (1,062 kilometers per hour).

56-6671 was taken back to the North American Aviation plant for repair. It returned to flight operations three months later.

Test pilot A. Scott Crossfield with the damaged X-15 (UPI/Harry Ransom Center
Test pilot A. Scott Crossfield with the damaged X-15 on Rosamond Dry Lake. (UPI/Harry Ransom Center, University of Texas at Austin)

© 2016, Bryan R. Swopes