Tag Archives: Airliner

29 December 1972

Eastern Airlines' Lockheed L-1011-385-1 TriStar, N310EA, the airliner that crashed 29 December 1972. (Photograph © Jon Proctor. Used with permission.)
Eastern Air Lines’ Lockheed L-1011-385-1 TriStar, N310EA. (Photograph © Jon Proctor. Used with permission.)

29 December 1972: Eastern Air Lines Flight 401, a Lockheed L-1011 TriStar, was en route from John F. Kennedy International Airport (JFK), New York, to Miami International Airport (MIA), Florida, with a crew of 13 and 163 passengers. The flight was under the command of Captain Robert Albin Loft, a 32-year-veteran of Eastern Air Lines. The co-pilot was First Officer Albert John Stockstill, a former U.S. Air Force pilot who had flown with Eastern as a flight engineer for 12 years before upgrading to first officer the previous year. The Second Officer (flight engineer) was Donald Louis Repo. He was employed as a mechanic by Eastern in 1947, and had qualified as a flight engineer in 1955.

On approach to MIA, the flight crew lowered the landing gear. The indicator light for the nose gear did not illuminate. Captain Loft informed the Miami control tower that he was abandoning the approach and requested a holding pattern. Miami Approach Control placed Flight 401 in a “race track” pattern at 2,000 feet (610 meters), west of MIA.

The flight crew confirmed that the landing gear was operating properly, and confirmed that the incandescent light bulb for the gear position indicator was burned out. Still, all three members of the flight crew, as well as a fourth Eastern Air Lines employee who was in the cockpit, continued to investigate the light’s malfunction. While they did so, the airplane entered a very gradual descent which went unobserved by the crew.

The following partial transcript is from the airplane’s Cockpit Voice Recorder:

Miami Approach Control: “Eastern, ah Four Oh One how are things comin’ out there?” [2341:40]

Eastern Air Lines Flight 401: “Okay, we’d like to turn around and come back in.” [2341:44]

Miami Approach Control: “Eastern Four Oh One turn left heading one eight zero.” [2341:47]

First Officer: “We did something to the altitude.” [2342:05]

Captain: “What?” [2342:05]

First Officer: “We’re still at two thousand, right?” [2342:07]

Captain: “Hey, what’s happening here?” [2342:07]

Radar Altimeter Altitude Alert: BEEP BEEP BEEP BEEP BEEP BEEP [2342:10]

(Sound of ground impact) [2342:12]

At 11:42:12 p.m., Eastern Standard Time, Flight 401 impacted the surface of an Everglades swamp, 18.7 miles (30.1 kilometers) west-northwest of the end of Runway 9L. The TriStar hit the ground at 227 miles per hour (365 kilometers per hour) in a 28° left bank. Of the 176 persons on board, 99 were killed and 75 were injured. 2 of the injured died later.

Wreckage of Eastern Airlines Flight 401.
Wreckage of Eastern Air Lines Flight 401.

The cause of the accident was “pilot error.” In the simplest terms, the flight crew failed in their primary responsibility to FLY THE AIRPLANE while they dealt with an inconsequential technical issue. At the time, this was the highest number of fatalities in an aircraft accident in the United States.

PROBABLE CAUSE: “The National Transportation Safety Board determines that the probable cause of this accident was the failure of the fight crew to monitor the flight instruments during the final 4 minutes of flight, and to detect an unexpected descent soon enough to prevent impact with the ground. Preoccupation with a malfunction of the nose landing gear position indicating system distracted the crew’s attention from the instruments and allowed the descent to go unnoticed.”

Aircraft Accident Report, Eastern Air Lines, Inc. L-1011, N310EA, Miami, Florida, December 29, 1972, Report Number NTSB-AAR-73-14, Adopted 14 June 1973, Chapter 2.2 at Pages 23–24

Following the crash of Eastern Air Lines Flight 401, and the similar crash of a United Air Lines DC-8, Flight 173, at Portland, Oregon, 28 December 1978, airlines developed a system called Cockpit Resource Management to ensure that the flight crews stayed focused on cockpit priorities while dealing with unexpected issues.

The cabin crew of Flight 401, 29 December 1972: Back row: Pat Ghyssels, Trudy Smith, Adrianne Hamilton, lead Flight Attendant, Mercy Ruiz. Front row: Sue Tebbs, Dottie Warnock, Beverly Raposa, Stephanie Stanich. Laying on the coat rack, Patty George. Not shown, Sharon Transue. Pat Ghyssels and Stephanis Stanich, seated next to each other in jump seats, were killed. (Sharon Transue/Eastern Airlines)
The cabin crew of Flight 401, 29 December 1972: Back row: Pat Ghyssels, Trudy J. Smith, Adrianne Ann Hamilton, lead Flight Attendant, Mercedes V. Ruiz. Front row: Sue F. Tibbs, Dorothy M. Warnock, Beverly Jean Raposa, Stephanie Stanich. Laying on the coat rack, Patricia R. Georgia. Not shown, Sharon R. Transue. Pat Ghyssels and Stephanie Stanich, seated next to each other in jump seats, were killed. (Sharon  R. Transue/Eastern Airlines)

Flight 401 was a Lockheed L-1011-385-1 TriStar, a long-range variant of the “wide body” airliner, FAA registration N310EA, (serial number N193A-1011) which had been delivered to Eastern Air Lines 18 August 1972 had entered service three days later. At the time of the crash it had just 986 hours total flight time (TTAF).

The L-1011 was a very technologically advanced airliner, operated by a flight crew of three, and could carry a maximum of 330 passengers. The –385 was 14 feet shorter than the previous TriStar versions, with a length of 164 feet, 2.5 inches (50.051 meters). It had longer wings, spanning 164 feet, 4 inches (50.089 meters). Its overall height was 55 feet, 4 inches (16.865 meters). Empty, it weighed 245,400 pounds (111,312 kilograms). The maximum takeoff weigh was 510,000 pounds (231,332 kilograms) and maximum landing weight, 368,000 pounds (166,922 kilograms).

N310EA was powered by three Rolls-Royce RB.211-22C turbofan engines, with two suspended on pylons under the wings and one in the rear of the fuselage. They produced 42,000 pounds of thrust (186.83 kilonewtons), each.

The L-1011-385-1 had a maximum speed of 0.95 Mach. Its cruising speed was 604 miles per hour (972 kilometers per hour). Range with maximum passengers was 6,151 miles (9,899 kilometers). The service ceiling was 43,000 feet (13,106 meters).

The Lockheed L-1011 was in production from 1968 to 1984. 250 of the airliners were built at Palmdale, California.

Eastern Airlines CEO, Frank F. Borman II (Gemini 7, Apollo 8) in the cockpit of a Lockheed L-1011 with Lockheed's test pilot Henry Baird ("Hank") Dees. (Eastern Airlines)
Eastern Air Lines CEO, Frank F. Borman II (Gemini 7, Apollo 8) in the cockpit of a Lockheed L-1011 with Lockheed’s test pilot Henry Baird (“Hank”) Dees. (Eastern Airlines)

© 2018, Bryan R. Swopes

26 December 1975

An Aeroflot Tupolev Tu-144S supersonic transport, CCCP-77106, loading cargo at Demodovo before its third commercial flight, 1976. (© Valeriy A. Vladimirov)
An Aeroflot Tupolev Tu-144S supersonic transport, CCCP-77106, loading cargo at Demodovo before its third commercial flight, 1976. (© Valeriy A. Vladimirov)

26 December 1975: The Tupolev Tu-144S, 004-1, operated by Aeroflot (OAO Aeroflot-Rossiyskiye avialinii) under civil registration CCCP-77106, was the first supersonic transport to enter commercial service when it flew a regularly-scheduled 2,010 mile (3,240 kilometer) route from Moscow Domodedovo Airport to Almaty, Kazakhstan, carrying mail and freight.

004-1 was the first production Tu-144S delivered to Aeroflot. A prototype and a pre-production Tu-144S had been built first. There were a total of 16 Tu-144s completed, with nine production Tu-144S and five Tu-144D models. The first production Tu 144S, CCCP-77102, broke up in flight at the Paris Air Show, 2 June 1973.¹

Passengers board Aeroflot's Tu-144S CCCP-77106, 1976. (© Valeriy A. Vladimirov)
Passengers board Aeroflot’s Tu-144S CCCP-77106, 1976. (© Valeriy A. Vladimirov)

The Tu-144S was built by Tupolev OKB at the Voronezh Aviation Plant (VASO), Pridacha Airport, Voronezh. It is a large double-delta-winged aircraft with a “droop” nose for improved low speed cockpit visibility and retractable canards mounted high on the fuselage behind the cockpit. It was flown by a flight crew of three and was designed to carry up to 120 passengers.

77106 is 65.50 meters (215 feet, 6.6 inches) long, with a wingspan of 28.00 meters (91 feet, 10.4 inches). The tip of the vertical fin was 11.45 meters (37 feet, 6.8 inches) high. The 144S has a total wing are of 503 square meters (5,414 square feet). Its empty weight is 91,800 kilograms (202,384 pounds) and the maximum takeoff weight is 195,000 kilograms (429,901 pounds). (A number of Tu-144S airliners had extended wing tips, increasing the span to 28.80 meters (94 feet, 5.9 inches) and the wing area to 507 square meters (5,457 square feet).

The Tu-144S was powered by four Kuznetsov NK-144A engines. The NK-144 is a two-spool axial-flow turbofan engine with afterburner. It uses a 2-stage fan section, 14-stage compressor section (11 high- and 3 low-pressure stages), and a 3-stage turbine (1 high- and 2 low-pressure stages). It is rated at 147.0 kilonewtons (33,047 pounds of thrust) for supersonic cruise, and 178.0 kilonewtons (40,016 pounds of thrust) with afterburner for takeoff. The NK-144A is 5.200 meters (17 feet, 0.7 inches) long, 1.500 meters (4 feet, 11.1 inches) in diameter and weighs 2,827 kilograms (6,233 pounds).

The 144S has a cruise speed of Mach 2.07 (2,200 kilometers per hour/1,367 miles per hour) with a maximum speed of Mach 2.35 (2,500 kilometers per hour/1,553 miles per hour). The service ceiling is approximately 20,000 meters (65,617 feet). Its practical range is 3,080 kilometers (1,914 miles).

In actual commercial service, the Tu-144 was extremely unreliable. It was withdrawn from service after a total of just 102 commercial flights, including 55 passenger flights.

004-1 made its first flight 4 March 1975 at Voronezh. On 29 February 1980, it made its 320th and final flight when it was flown to the Central Air Force Museum of Russia at Monino, Russia. The airframe has a total flight time of 582 hours, 36 minutes.

Tupolev Tu-144S 004-1, CCCP-77106, at the Central Aviation Museum Monino. (© Danner Gyde Poulsen)
Tupolev Tu-144S 004-1, CCCP-77106, at the Central Aviation Museum Monino. (© Danner Gyde Poulsen)

¹ https://www.thisdayinaviation.com/3-june-1973/

© 2023, Bryan R. Swopes

13 December 1955

DH.106 Comet 3 G-ANLO is decorated with a flower lei on its arrival at Honolulu International Airport, 13 December 1955. (Zoggavia)
De Havilland DH.106 Comet 3 G-ANLO is decorated with a flower lei on its arrival at Honolulu International Airport, 13 December 1955. (Zoggavia)

13 December 1955: The first landing of a commercial jet airliner on United States territory took place when a de Havilland DH.106 Comet 3, G-ANLO, flown by de Havilland’s chief test pilot, John Cunningham, with co-pilot Per Buggé, arrived at Honolulu International Airport, on the Island of Oahu, Territory of Hawaii.

The Comet 3 was on an around-the-world tour. The 3,212 mile (5,169 kilometer) flight from Nadi, Fiji (NAN) to Honolulu (HNL) took 6 hours, 41 minutes. The Comet remained at Hawaii for two days and gave a series of demonstration flights before continuing on its journey. The next leg, to Vancouver, British Columbia, Canada, a distance of 2,771 miles (4,460 kilometers), took 5 hours, 40 minutes.

De Havilland DH.106 Comet 3 G-ANLO ay the Farnborough Airshow, September 1954. (RuthAS via Wikipedia)
De Havilland DH.106 Comet 3 G-ANLO at the Farnborough Airshow, September 1954. (RuthAS via Wikipedia)

The de Havilland DH.106 Comet 3 was a further development of the Comet 2 series. It was 15 feet (4.572 meters) longer with a length of 111 feet, 6 inches (33.985 meters), a wingspan of 115 feet (35.052 meters) and overall height of 29 feet, 6 inches (8.992. The area of the wings and tail surfaces had been increased. It was powered by four Rolls Royce Avon 521 turbojet engines, rated at 10,000 pounds of thrust, each.

The airliner was designed to carry 58–76 passengers on flights ranging to 2,600 miles (4,184 kilometers). In addition to the increased length, visual differences from the previous Comets were the circular passenger windows, and wing tanks extending forward from the wings’ leading edges.

De Havilland DH.106 Comet 3 G-ANLO, left quarter, at Entebbe Airport, Uganda, 1955. (Dphne Seager)
De Havilland DH.106 Comet 3 G-ANLO, left quarter, at Entebbe Airport, Uganda, 1955. (Daphne Seager)

Only two Comet 3s were built and one was used as a static test article. Production continued with the Comet 4, which had even greater improvements. G-ANLO remained a development prototype and was modified several times. It was turned over to the Ministry of Supply and re-registered XP915. The airplane was used in instrument landing tests and later converted to a mockup of the Hawker Siddeley Nimrod MR1 maritime patrol aircraft. It was taken out of service in 1973.

Group Captain John Cunningham C.B.E., D.S.O. and Two Bars, D.F.C. and Bar, A.E., was the highest scoring Royal Air Force night fighter pilot of World War II, credited with shooting down 20 enemy airplanes. He was responsible for the myth that eating carrots would improve night vision.

Group Captain John Cunningham, Royal Air Force. (Daily Mail)
Group Captain John Cunningham, Royal Air Force, 1917–2002. (Daily Mail)

© 2015, Bryan R. Swopes

1 December 1984

NASA 833, a remotely-piloted Boeing 720 airliner, pulls up after a practice approach to the impact point on Rogers Dry Lake. The "X" is the planned touchdown point. The "rhino" barriers are at the runway threshold. (NASA)
NASA 833, a remotely-piloted Boeing 720 airliner, pulls up after a practice approach to the impact point on Rogers Dry Lake. The “X” is the planned touchdown point. The “rhino” barriers are at the runway threshold. (NASA)

After four years of planning and preparation, the National Aeronautics and Space Administration (NASA) and the Federal Aviation Administration (FAA) intentionally crashed a Boeing 720 airliner to test an experimental fuel additive intended to reduce post-crash fires, and to assess passenger survivability. An anti-misting agent was added to standard commercial JP-5 jet fuel to create AMK, or “Anti-Misting Kerosene.” The airliner’s fuel tanks were filled with the AMK mixture, totaling 16,060 gallons (10,794 liters). Instrumented crash test dummies were placed in the passengers seats.

Passengers relaxing before a flight aboard NASA’s Boeing 720, N833NA. (NASA ECN-28307)

NASA 833, the Boeing 720-027 airliner, FAA registration N833NA, was a remotely-piloted aircraft. NASA test pilot Fitzhugh Lee (“Fitz”) Fulton, Jr., flew NASA 833 from a ground station, the NASA Dryden Remotely Controlled Vehicle Facility. More than 60 flights had been made prior to the actual test.

Fitz Fulton in the CID.
Fitz Fulton in the NASA Dryden Remotely Controlled Vehicle Facility

The test was planned so that the airliner would make a shallow 3.8° approach to a prepared runway on the east side of Rogers Dry Lake at Edwards Air Force Base. It was to land on its belly in a wings-level attitude, then slide into a group of barriers, called “rhinos,” which would slice open the wing tanks. The fuselage and passenger cabin would remain intact. NASA and the FAA estimated that this would be “survivable” for all occupants.

Just before touchdown, the Boeing 720 entered a "Dutch roll." The airliner's nose yawed to the left and the left wing dipped, striking the ground sooner than was planned. All four engines are still at full throttle. NASA 833 is to the right of the runway center line. (NASA)
Just before touchdown, the Boeing 720 entered a “Dutch roll.” The airliner’s nose yawed to the left and the left wing dipped, striking the ground sooner than was planned. All four engines are still at full throttle. NASA 833 is to the right of the runway center line. (NASA)

As the Boeing 720 descended on its Final Approach, its nose yawed to the right and the airplane went to the right of the runway center line. It then yawed back to the left and entered an out-of-phase oscillation called a “Dutch roll.” The decision height to initiate a “go-around” was 150 feet (45.7 meters) above the surface of the lake bed. Fitz Fulton thought he had enough time to get NASA 833 back on the center line and committed to the test landing. However, the Dutch roll resulted in the airliner’s left wing impacting the ground with the inboard engine on the left wing (Number Two) just to the right of the center line.

NASA 833 slews left as it approaches the test apparatus. The Boeing 720 has reached the intended touchdown point but is out of position, still to the right of center line and misaligned. (NASA)
NASA 833 slews left as it approaches the test apparatus. The Boeing 720 has reached the intended touchdown point but is out of position, still to the right of center line and misaligned. (NASA)

According to the test plan, all four of the airliner’s engines should have been brought to idle, but they remained at full throttle. The left wing’s impact yawed the airliner to the left and, rather than the fuselage passing through the rhino barriers undamaged, the passenger compartment was torn open. Another rhino sliced into the Number Three engine (inboard, right wing), opening its combustion chamber. With the fuel tanks in the wings ruptured, raw fuel was sprayed into the engine’s open combustion chamber which was still at full throttle.

 As the airliner slides through the "rhino" barriers, they rip open the fuel tanks, the Number Three engine and the passenger compartment. The raw fuel immediately ignited. (NASA)
As the airliner slides through the “rhino” barriers, they rip open the fuel tanks, the Number Three engine and the passenger compartment. The raw fuel immediately ignited. (NASA)

The raw fuel ignited and exploded into a fireball. Flames immediately entered the passenger compartment. As the 720 slid on the runway it continued to rotate left and the right wing broke off though the fuselage remained upright.

NASA 833's right wing breaks off, rupturing the fuel tanks. Nearly 8,000 gallons (30,000 liters) of jet fuel pours out into the fireball. (NASA)
NASA 833’s right wing breaks off, rupturing the fuel tanks. Nearly 8,000 gallons (30,000 liters) of jet fuel pours out into the fireball. (NASA)

As the right wing came off the ruptured fuel tanks emptied most of the raw fuel directly into the fireball.

The flaming wreckage of NASA 833 slides to a stop on Rogers Dry Lake. Fire fighters needed more than one hour to extinguish the fire. (NASA)
The flaming wreckage of NASA 833 slides to a stop on Rogers Dry Lake. Fire fighters needed more than one hour to extinguish the fire. (NASA)

Over an hour was required to extinguish the flames. The test of the flame-reducing fuel additive was a complete failure. Test engineers estimated that 25% of the occupants might have survived the crash, however, it was “highly speculative” that any could have escaped from the burning, smoke-filled passenger compartment.

Fithugh L. "Fitz" Fulton, Jr. (NASA)
Fitzhugh Lee “Fitz” Fulton, Jr., with NASA 905, a Shuttle Carrier Aircraft, and Enterprise (OV-101). (NASA)
Fitz Fulton, 1942 (The Cohiscan)

Fitzhugh Lee Fulton, Jr., was born at Blakely, Georgia, 6 June 1925, the first of two sons of Fitzhugh Lee Fulton, a merchant seaman, and Manila Fulton. He attended Columbus High School, Columbus Georgia, graduating in 1942. He entered College at Alabama Polytechnic Institute (now known as Auburn University) and the University of Oklahoma. He was awarded a bachelor of arts degree from Golden Gate University, San Francisco, California.

Fulton entered the U.S. Army Air Corps in 1943, and was trained as a pilot. He married Miss Erma I. Beck at Tucson, Arizona, 16 December 1945. They would have three children.

Following World War II, participated in Operation Crossroads, the atomic bomb tests at Bikini Atoll, July 1946. Lieutenant Fulton flew the Douglas C-54 Skymaster four-engine transport during the Berlin Airlift, making 225 sorties, and then the Douglas B-26 Invader light attack bomber during the Korean War.

Captain Fitz Fulton, U.S. Air Force, in teh cockpit of a Douglas B-26 Invader, circa 1952. (Air & Space Magazine)
Captain Fitz Fulton, U.S. Air Force, in the cockpit of a Douglas B-26 Invader, circa 1952. (Air & Space Magazine)

Fulton graduated from the Air Force Test Pilot School in 1952. He served as project test pilot for the Convair B-58 Hustler supersonic bomber and flew the B-58 to a World Record Altitude of 26,017.93 meters (85,360.66 feet) on 14 September 1962.¹

Major Fitz Fulton in the cockpit of a Convair B-58. (Jet Pilot Overseas)
Major Fitz Fulton in the cockpit of a Convair B-58. (Jet Pilot Overseas)

At Edwards Air Force Base, he flew the B-52 “mother ships” for the X-15 Program. He flew the North American XB-70A Valkyrie faster than Mach 3. When Fulton retired from the Air Force in 1966, he was a lieutenant colonel assigned as Chief of Bomber and Transport Test Operations.

Fitz Fulton continued as a research test pilot for NASA, flying as project pilot for the YF-12A and YF-12C research program. He flew all the early test flights of the NASA/Boeing 747 Shuttle Carrier Aircraft and carried the space shuttle prototype, Enterprise. By the time he had retired from NASA, Fulton had flown more than 16,000 hours in 235 aircraft types.

Fitzhugh L. Fulton, Jr., died at Thousand Oaks, California, 4 February 2015, at the age of 89 years..

Lieutenant Colonel Fitzhugh Lee Fulton, Jr., with a North American Aviation XB-70A Valkyrie.
Colonel Joseph Frederick Cotton and Lieutenant Colonel Fitzhugh Lee Fulton, Jr., with a North American Aviation XB-70A Valkyrie.

NASA 833 (c/n 18066) was ordered by Braniff Airways, Inc., as N7078, but the sale was not completed. The airplane first flew 5 May 1961 and it was delivered to the Federal Aviation Administration as a test aircraft one week later, 12 May 1961, registered N113. A few years later the identification was changed to N23, then back to N113, and then once again to N23. In 1982, the Boeing 720 was transferred to NASA to be used in the Controlled Impact Demonstration. At this time it was registered as N2697V. A final registration change was made to N833NA.

NASA 833 at Edwards Air Force Base, prior to the Controlled Impact Demonstration. (Paul)

The Boeing 720 was a variant of the Model 707, intended for short to medium range flights. It had 100 inches (2.54 meters) removed from the fuselage length and improvements were made to the wing, decreasing aerodynamic drag, though it retained the span of the 707.

The Boeing 720 was powered by four Pratt & Whitney Turbo Wasp JT3C-7 turbojet engines, a civil variant of the military J57 series. The 720B was equipped with the more efficient P&W JT3D-1 turbofan engines. The JT3C-7 was a “two-spool” axial-flow engine with a 16-stage compressor (9 low- and 7 high-pressure stages), 8 combustion tubes, and a 3-stage turbine (1 high- and 2 low-pressure stages). It was rated at 12,030 pounds of thrust (53.512 kilonewtons) for takeoff. The JT3D-1 was a dual axial-flow turbofan engine, with a 2-stage fan section 13-stage compressor (6 low- and 7 high pressure stages), 8 combustion chambers and a 4-stage turbine (1 high- and 3 low-pressure stages). This engine was rated at 14,500 pounds of static thrust (64.499 kilonewtons) at Sea Level, and 17,000 pounds (75.620 kilonewtons), with water injection, for takeoff (2½ minute limit). Almost half of the engine’s thrust was produced by the fans. Maximum engine speed was 6,800 r.p.m. (N1) and 10,200 r.p.m. (N2). It was 11 feet, 4.64 inches (3.471 meters) long, 4 feet, 5.00 inches (1.346 meters) wide and 4 feet, 10.00 inches (1.422 meters) high. It weighed 4,165 pounds (1,889 kilograms). The JT3C could be converted to the JT3D configuration during overhaul.

The maximum cruise speed of the Boeing 720 was 611 miles per hour (983 kilometers per hour) and maximum speed was 620 miles per hour (1,009 kilometers per hour). The range at at maximum payload was 4,370 miles (7,033 kilometers).

Boeing built 154 720 and 720B airliners from 1959 to 1967.

The Federal Aviation Administration's Boeing 720-027 N113. (FAA)
The Federal Aviation Administration’s Boeing 720-027 N113. (FAA)

¹ FAI Record File Numbers 14652 and 14656

© 2018, Bryan R. Swopes

23 November 1959

Boeing 720-022 c/n 17907, N7201U. (Boeing)
Boeing 720-022 c/n 17907, N7201U, parked on the taxiway at the south shore of Lake Washington. (Boeing)

23 November 1959: The first Boeing 720 airliner, a 720-022, registered as N7201U, made its first flight at Renton, Washington. The 720 was a development of the 707 and no prototype was built. N7201U was used by Boeing for flight testing and was then delivered to United Airlines, 1 October 1960. The airline named the new 720 Jet Mainliner Capt. F. M. Crismore. Over the next two years, United acquired 29 Boeing 720s.

N7201U was sold to Contemporary Entertainment, owned by singer Bobby Sherman and his manager, Ward Sylvester, in January 1973. It was repainted in a gold and black livery and christened The Starship. As a VIP transport, it was used by such rock bands as Led Zeppelin, Deep Purple, The Rolling Stones, Alice Cooper and Elton John. It was last chartered by Peter Frampton.

N7201U was withdrawn from service in 1977 and after being stored for several years, was broken up at Luton Airport near London, England, in 1982.

The Boeing 720 was a variant of the Model 707, intended for short to medium range flights. It had 100 inches (2.54 meters) removed from the fuselage length and improvements to the wing, decreasing aerodynamic drag.

Boeing built 154 720 and 720B airliners from 1959 to 1967.

The Boeing 720 was operated by a flight crew of four and could carry up to 149 passengers. It was 136 feet, 2 inches (41.25 meters) long with a wingspan of 130 feet, 10 inches (39.90 meters) and overall height of 41 feet, 7 inches (12.65 meters). The airplane had an empty weight of 103,145 pounds (46,785 kilograms) and Maximum Takeoff Weight of 220,000 pounds (100,800 kilograms).

The Boeing 720 was powered by four Pratt & Whitney Turbo Wasp JT3C-7 turbojet engines, a civil variant of the military J57 series. The 720B was equipped with the more efficient P&W JT3D-1 turbofan engines. The JT3C-7 was a “two-spool” axial-flow engine with a 16-stage compressor (9 low- and 7 high-pressure stages), 8 combustion tubes, and a 3-stage turbine (1 high- and 2 low-pressure stages). It was rated at 12,030 pounds of thrust (53.512 kilonewtons) for takeoff.

The JT3D-1 was a dual axial-flow turbofan engine, with a 2-stage fan section 13-stage compressor (6 low- and 7 high pressure stages), 8 combustion chambers and a 4-stage turbine (1 high- and 3 low-pressure stages). This engine was rated at 14,500 pounds of static thrust (64.499 kilonewtons) at Sea Level, and 17,000 pounds (75.620 kilonewtons), with water injection, for takeoff (2½ minute limit). Almost half of the engine’s thrust was produced by the fans. Maximum engine speed was 6,800 r.p.m. (N1) and 10,200 r.p.m. (N2). It was 11 feet, 4.64 inches (3.471 meters) long, 4 feet, 5.00 inches (1.346 meters) wide and 4 feet, 10.00 inches (1.422 meters) high. It weighed 4,165 pounds (1,889 kilograms). The JT3C could be converted to the JT3D configuration during overhaul.

The maximum cruise speed was 611 miles per hour (983 kilometers per hour) and maximum speed was 620 miles per hour (1,009 kilometers per hour). Range at at maximum payload was 4,370 miles (7,033 kilometers).

The last flight of a Boeing 720 was on 9 May 2012, when a 720B aircraft used by Pratt and Whitney Canada as a test aircraft was placed in the National Air Force Museum of Canada at Trenton, Ontario.

United Airlines' Boeing 720-022, N7201U. (Unattributed)
United Airlines’ Boeing 720-022, N7201U. The airliner’s name, “Jet Mainliner Capt. F. M. Crismore,” is visible under the cockpit windows. (Bill Larkins via Wikipedia)

© 2018, Bryan R. Swopes